eltham well hall train crashcar accident in hartford, ct today
Running slightly late and at Wilsdon's urging, the pair returned to Ramsgate Depot at around 19:40. Eltham Well Hall is seen in this Dartford-bound view less than a year before closure. Press Association. This caused nine out of 10 carriages to derail, injuring many occupants and killing 6 including the driver. Stokes was 18 years old and had been working on the railways for almost two years at the time of the accident, having been based at Hither Green this entire time. By the time the train approached Eltham Well Hall station it was running at around 65mph. Except where otherwise indicated, Everything.Explained.Today is Copyright 2009-2022, A B Cryer, All Rights Reserved. The name "Well Hall" derived from that of a former Tudor mansion, which resided on a site surrounded by a moat, located 160-yards north of the station. The last recommendation that Robertson made regarding the accident was the usage of telephone to sign on duty within the Southern Region. Transport Libraries The last station the train passed on its journey that Atterbury had to time was at Bexleyheath railway station 4.3miles east of the accident site. Latest Documents This was another recommendation that had previously been made - this time in 1972 in the aftermath of the Eltham Well Hall rail crash, in which six people died following a derailment caused by driver Robert . All three of these coaches were leaning over on their left sides to various degrees, with the leading end of the fifth coach having been badly damaged by the impact with the fourth coach. The actions of his superior regarding this incident were criticised as "unwise" but were not considered a serious failing. A combination of the signal checks at Sittingbourne and Rainham and the unscheduled stop at Rainham had caused Wilsdon to lose most of the progress he had made between Margate and Sittingbourne. Arundell believed that they were a gift left by the organisers of the excursion to the engine crew - such being a normal 'tip' for excursion drivers to enjoy off-duty - and he did not question their appearance. The second uncertain moment was what occurred to both him and Stokes during the stop at Margate, in which both seemingly left the station via the Platform No.1 entrance. Pinterest. The closure of Eltham Park in connection with the road scheme was formally approved on 26th March 1984. A second trailing crossover between the running lines had been installed 50-yards east of the platforms, and the goods yard acquired a further two sidings and a shed (although, as per that at Bexleyheath, rails did not pass through it). The original document format was Stapled Book, and comprised 27 pages. According to Obee, Wilsdon had stopped at Rainham to inquire of the position of the first excursion train, which Obee explained was to stop at Gillingham railway station and would let Wilsdon overtake it, which was not as planned (Wilsdon's train was to overtake the first excursion train at Newington railway station which was prior to Rainham); to which Wilsdon told him "you should read your weekly notices". Despite this, Wilsdon suggested the pair go to the nearby Railway Staff Association Club at about 19:00 and get a drink to which Stokes agreed, with the pair arriving just in time for the club to open at 19:05. 11 June 1972: D1630 was involved in the notorious Eltham Well Hall rail crash in which six people were killed. The structure sat at milepost 9 from Charing Cross. At no point did Wilsdon even attempt to slow his train beyond having already shut off the engine to coast which was normal at this long downhill sector of the line. This caused both coaches to overturn onto their right side, with the leading end of the second coach coming to a stand in front of the locomotive and the rear of the first coach, which in combination with the fourth coach, formed an "N" shape with the first four coaches. Stokes was unable to recall much of what occurred at Margate and Wilsdon died, so it was uncertain as to what had occurred during this period, and although a pub was close to the station, it was considered that they did not have enough time to reach it. Both Wilsdon and his colleague were reinstated on 18 December 1961, with Wilsdon being promoted to driver less than a week later on 25 December with his transfer to Hither Green. He later commented to Stokes a joking complaint about the driver of the first excursion train, calling him a "slow bastard". The only other theory was that Wilsdon had obtained a bottle of spirits at some point, stored it on his person and had drunk it at some point after leaving Margate, and later disposed of the glass by throwing it out the window of the locomotive, with the theory being that Wilsdon either obtained the bottle at some point whilst in Margate or had kept one on his person since he left Rainham for work. 47048), came off the rails. Eltham,Well,Hall,rail,crashThe,Eltham,Well,Hall,rail,crash,was,an,accident,on,the,British,railway,system,that,occurred,on,11,June,1972,at,approximately,21:35. Both were severely damaged. Single-storey they may have been, but these were substantial main buildings for these intermediate stations, extending for 145-feet in length, with widths of 20-feet and 25-feet at their narrowest and widest points respectively. As well as Wilsdon, two passengers died at the scene; a woman later died of her injuries in August and a male likewise in November, bringing the number of fatalities to five. A small goods yard was situated behind the London end of the "up" platform, comprising two sidings, one of which terminated at a "dock" platform. He subsequently gave Wilsdon a stern reprimand and advised him that such behaviour was not acceptable. An excursion train returning from Margate came off the track on the sharp curve outside the station. Computations later proved that the driver had apparently shut off power where required, but had not made a brake application. He briefed the pair on the train's particulars with Wilsdon appearing sober and routine. Railman Fleming, who was on duty at the platform and knew Wilsdon well, saw the train arrive and asked Wilsdon if it had broken down (owing to the clear signal visible from the platform), to which Wilsdon merely said "No" and jumped down from his cab before walking to a telephone on the platform to speak with Obee. He was thoroughly critical of Wilsdon's behaviour, describing it as "reprehensible" and "disgraceful". Contributions Whilst it was agreed that it was a fairly common occurrence in the Southern Region and British Rail had adopted a policy where certain drivers could be granted need to book on via telephone (typically those either living far from depots or those whose duties commenced far from their depots). By the time the train approached Eltham Well Hall station it was running at around 65 miles per hour (105km/h). An excursion train from Margate to Kentish Town derailed on a sharp curve at Eltham Well Hall station, Eltham, London. However, changes were made to the signalling at Eltham so that through trains would receive a yellow signal on approach. A 24-year-old man was cut free from wreckage crushing his head and abdomen and died from a heart attack on the way to hospital. This did not occur, and the two met up at Ramsgate Depot by the locomotive at around 18:25. Your author surmises it was during this incident that the up side platform canopy was damaged. Wilsdon met with his secondman, a youth of 18 years, there. The second incident occurred on 28 March 1969, when Wilsdon was fined 1 for being drunk in Lewisham. On Sunday 11th June 1972 at 21:36, disaster struck. Photograph by Press Association, 1972. Today. Physical description 1 photograph : photoprint ; sheet 15.3 x 20.2 cm Contributors According to his notes, the train passed through Bexleyheath at 21:31, seven minutes behind schedule (estimates showed that Wilsdon had made up at least a minute and a half between Gillingham and Strood) and was running on clear signals.[2]. As well as Wilsdon, two passengers died at the scene; a woman later died of her injuries in August and a male likewise in November, bringing the number of fatalities to five. The first and most serious of these moments was the fact that it was uncertain what had occurred with Wilsdon and his brothers between 14:02 and 17:15 with his brothers both declaring that Wilsdon had not drunk after returning from the pub in Rainham. Explore. Emergency services were notified, and arrived between 21:40 and 21:42. Stationmaster Arundell signalled the train clear to depart for London, but both he and Atterbury found that there was no response in the cab. All witnesses who saw the driver including the guard, the station staff at both Rainham and Margate, and the depot staff at Ramsgate, observed no signs of intoxication. Eltham Eltham station Well Hall Road Eltham Greater London SE9 6SL GET DIRECTIONS Ticket office opening hours: Monday - Friday - 06:40 to 20:00 Saturday - 06:10 to 20:00 Sunday - 08:10 to 15:40 NO Waiting room YES Ticket machine YES Toilet YES Impaired Access Staff Station facilities Ticketing Services & Information Oyster Pre-Pay YES Yes 1630 (latterly Class 47 No. Book: Ministry of Transport . At 19:45 they met with the guard and drove the train to Margate to receive the passengers. The driver of the Excursion train was Robert Wilsdon, a Driver for British Rail's Southern Region based at Hither Green TMD since December 1961. Apr 2, 2017 - Eltham Well Hall Rail Crash. The first occurred on 7 November 1961, when Wilsdon had been charged 150 for being Drunk and disorderly, causing damage to a shop window and assaulting a Police constable whilst off-duty. Those who knew the driver said that he was quite a frequent drinker of alcohol and could "carry" much beer. Further modernisation was the order of the day in 1931, when stations at Bexleyheath, Welling, and Eltham (Well Hall) were rebuilt. In the cab, Stokes later recalled that Wilsdon had suddenly shouted in a frightened way at the sight of the curve approaching, to which Stokes immediately braced himself in the seconds that he had available. When autocomplete results are available use up and down arrows to review and enter to select. At 15:22 Wilsdon signed on duty with Hither Green by telephone. Its nameplates were salvaged, and transferred to No. The driver Robert Wilsdon and five passengers were killed, and 126 people were injured. Robertson, concluded that the driver Robert Wilsdon had "grossly impaired his ability to drive safely by drinking a considerable quantity of alcohol both before and after booking on duty, including some shortly before leaving Margate and some more in his cab during the journey.". A medical expert stated that during the time given, 5 pints of bitter, a third of a bottle of sherry and a quarter bottle of spirits would "just about achieve" the levels found, providing that "the bulk of the spirits was drunk between 20:15 and 21:30". Temporary public electric workings operated down all three routes between 10th and 16th May 1926 inclusive, as a result of the General Strike, steam-hauled passenger trains briefly resuming afterwards. Although Robertson could not confirm Stokes' statements, he considered it likely that Wilsdon had drunk after 14:02 owing to the smell on Wilsdon's breath at Rainham several hours later and, whilst not explicitly accusing Wilsdon's brothers of lying, considered that anybody who tried to hide evidence of Wilsdon's drinking that day "did him a disservice". He made recommendations that booking-on of drivers by telephone should be controlled carefully, but did not recommend any changes to warnings of permanent speed restrictions. A concrete-lined cutting accommodating a dual-carriageway was envisaged, this of which would run parallel with the Bexleyheath Line for about a mile in the vicinity of Eltham, before passing under the railway at Well Hall. His suspension in 1961 was considered a warning sign of Wilsdon's alcoholic tendencies but it was agreed that at the time there was no evidence to disprove Wilsdon's statements that he would better himself and not drink again. The adequacy of the taxonomy is discussed with regards to the socio-technical context of accident reports. Shortly thereafter, Wilsdon and Stokes returned and entered the cab preparing for departure, with neither seeming unusual: when Arundell told them to hurry up, Wilsdon calmly noted they could regain lost time on the journey. Closure of Eltham Well Hall and Eltham Park stations was scheduled for Saturday 2nd March 1985, when the new platforms east of the former would be brought into use with a huge interchange with bus services. The final uncertainty was the fact that when his body was autopsied, Wilsdon's blood alcohol content was 0.278% (the legal limit for driving a road vehicle in England at that time was 0.08%). Creative Commons Attribution 4.0 International Licence. In the meantime, the Bexleyheath, Dartford Loop, and North Kent Lines were electrified using the SRs favoured 660-Volts DC third rail system. Before he could go ask superiors as to where they were, he saw Stokes and Wilsdon return. Stokes was unable to recall much of what occurred at Margate and Wilsdon died, so it was uncertain as to what had occurred during this period, and although a pub was close to the station, it was considered that they did not have enough time to reach it. Along this paper, the methodology is exemplified on a specific accident: the derailments caused by over-speed in curve. Although Atterbury had been somewhat concerned about excessive speed between Gillingham and Chatham, he stated that Wilsdon had operated appropriately through Dartford. The same design came into use at all three stations: a single-storey red brick structure with a hipped tiled roof, complemented with an upward-sloping canopy with plain valance. From 1st October 1916, the station was known as Well Hall and North Eltham. The journey was normal until the train stopped for signals at Rainham, whereafter the driver made an unscheduled stop in the station to telephone the signalman and ask about another excursion train that they were due to pass some distance ahead. It seems these splashes were too late and light to register in the cab. I much regret to report that five passengers in the train and its driver lost their lives and that 126 people, including the secondman on the locomotive, were injured and were either taken to hospitals in the area or received medical attention at the site of the accident: 40 of those taken to hospital were detained, some of them being very seriously injured. Railman Akehurst, who was on duty on the Well Hall platforms, had seen several earlier trains pass through the station and thence the curve, all of them slowing to the safe speed of 20 miles per hour (32km/h) but when he saw the excursion train approaching, he was quite certain it was traveling far beyond that speed. Wilsdon met with his secondman, a youth of 18 years, there. The train was an excursion for Kentish Town-based railway employees of the London Midland Region and their families. The train passed through at high speed without braking and sped into the curve at around 65 miles per hour (105km/h). Both brothers confirmed that he had not drunk after leaving the pub and were adamant on this point at the later public inquiry. Both men were subsequently suspended shortly afterwards, against which Wilsdon immediately appealed, claiming that the event was an isolated incident. This evidence contradicts that of Wilsdon's brothers who claimed that he had not drunk between 14:02 and 17:15. Upon completing his phone conversation, Wilsdon returned to his cab and departed having been stopped at Rainham for about four minutes. Further Research Well Hall was located exactly nine miles from Charing Cross upon an 86-chain curve, descending at 1 in 120 in the London direction. Guard Atterbury, who arrived at Ramsgate some hours earlier and had been relaxing in the staff break room of the station, had gone to prepare the train for its departure at around 19:30 and initially noted that the engine crew were absent. The guard told the inquiry that after leaving Rainham he had noticed that the train's speed has been "a little bit excessive" and that the driver braked intensely between Gillingham and Chatham. Please see this explanation for further details. He claimed that he was going to head directly to Ramsgate from Rainham and said that he had to catch an earlier train from Rainham (the 15:32 instead of the 15:42, which was not running on Sundays) and therefore asked Hither Green if he could be considered on-duty from 15:12. He was not suspended for this incident owing to the fact that his superior at Hither Green was busy and then went on leave and as such was not able to speak with Wilsdon until June. Despite his experience and long time working on the railways, Wilsdon had been reprimanded five times throughout his career. An excursion train from Margate to Kentish Town derailed on a sharp curve at Eltham Well Hall station, Eltham, London. This caused both coaches to overturn onto their right side, with the leading end of the second coach coming to a stand in front of the locomotive and the rear of the first coach, which in combination with the fourth coach, formed an "N" shape with the first four coaches. 125 passengers were injured.[2]. 125 passengers were injured. Website & Copyright information - Links - Contact the Webmaster, All content is copyright David Glasspool unless otherwise stated. He later commented to Stokes a joking complaint about the driver of the first excursion train, calling him a "slow bastard". Depending on the status and age of the original document, you may need an OPSI click-use license if you wish to reproduce this material, and other restrictions may apply. By 1972 he was married with young children and living in Rainham, Kent - which meant he would usually have to make an almost two hour rail commute to his depot at Hither Green. Notable survivors of the 1931 rebuilding at all three stations mentioned were the SER timber waiting shelters. All witnesses who saw the driver including the guard, the station staff at both Rainham and Margate, and the depot staff at Ramsgate, observed no signs of intoxication. The Eltham Well Hall rail crash was an accident on the British railway system that occurred on 11 June 1972 at approximately 21:35. The rear of the coach had been somewhat damaged by the fifth, sixth and seventh coaches passing by it, derailed but still on the track. A track foot crossing for staff remained in place, this of which was situated roughly midway down the platforms and required climbing on small steps to access. Investigating this theory, the morning after the accident, the cab was searched and three smashed glasses were found in the cab's wreckage. A third smashed bottle found was later proven to have been a medicine bottle and was unlikely to have carried any alcohol at the time of the accident. Eltham Well Hall rail crash a train derailedderailed on a sharp curve at Eltham Well Hall stationEltham (Well Hall) derailmentLondon-bound train came off the track The Eltham Well Hall rail crash was an accident on the British railway system that occurred on 11 June 1972 at approximately 21:35.wikipedia 47Related Articles [filter] June 11, 1972. Poor weather hampered construction and pushed back the commissioning of the new station, both the existing sites lingering on until Saturday 16th March 1985. Pictures by my father, Reg Godsave. derailment. injuries= 126The Eltham Well Hall rail crash was an accident on the British railway system that occurred on 11 June 1972 at approximately 21:35. A post-mortem examination of Wilsdon showed that he had a blood alcohol level of 0.278% (the legal limit for driving a road vehicle is 0.08%). There was an imbalance with the urine alcohol level which made it very likely that the driver had also been drinking alcohol at the controls. This issue was however was brought up again in 1991 after the Cannon Street station rail crash in which the driver in that instance was believed to have been high on cannabis and caused a buffer-stop collision. The Eltham Well Hall rail crash was an accident on the British railway system that occurred on 11 June 1972 at approximately 21:35. Robertson . Having left Margate eight minutes late and scheduled to run non-stop (aside from a later stop to change crew), Wilsdon was able to run the train at high speed and according to Atterbury's timings, was only a minute late after passing Faversham (24 miles (39km) from Margate). ", -- More Tools -- The Eltham Well Hall rail crash was an accident on the British railway system that occurred on 11 June 1972 at approximately 21:35. He stated that he was thoroughly ashamed and that he had been celebrating a promotion to the position of Passed Fireman with his colleague who greatly assisted him. All three of these coaches were leaning over on their left sides to various degrees, with the leading end of the fifth coach having been badly damaged by the impact with the fourth coach. It will be noticed on those structures which still survive at Bexleyheath and Welling that their wider, 25-foot portions also demonstrate a higher hipped roof section. Two bottles of beer given to the crew by the excursion's organisers were found in the cab, but they were unopened. None of the staff were criticised for failing to stop Wilsdon from his duties under the belief he was too drunk and evidence by Wilsdon's father-in-law, brothers and friends confirmed that although Wilsdon did drink heavily, he could "carry" his alcohol well and that the amount of alcohol he drank was not enough to make his drunkenness visible, although the report believed that Wilsdon's actions at Rainham and his reactions at Eltham Well Hall clearly showed that he was beginning to suffer effects of drunkenness. The scheme required the demolition of Well Hall station, for it partially resided on the site required for the trunk road, but also gave rise to the closure of Eltham Park station and the provision of a brand new set of platforms in-between the two. It also meant that his Supervisors at Hither Green would not see him in person. However, changes were made to the signalling at Eltham so that through trains would receive a yellow signal on approach. The train passed through at high speed without braking and sped into the curve at around 65mph. Those who knew the driver said that he was quite a frequent drinker of alcohol and could "carry" much beer. Despite this, Robertson felt that there was no severe issue with drinking amongst drivers on Britain's railways, with only two other accidents (one in 1913 and another in 1952) having occurred explicitly due to driver drunkenness in the sixty years prior to the accident, and as such he believed that it was a combination of railway staff's thoughts and self-discipline for drivers' behaviour with alcohol. An excursion train from Margate to Kentish Town derailed on a sharp curve at Eltham Well Hall station, Eltham, London. That day the Harrow Observer reported the horrific accident and 66 years later, getwestlondon pays tribute to the victims. Well Hall is a place to the north of Eltham in the Royal Borough of Greenwich in southeast London, England, with no present formal boundaries and located 13.5 km (8.4 mi) east-southeast of Charing Cross. Before he could go ask superiors as to where they were, he saw Stokes and Wilsdon return. The Eltham Well Hall rail crash was an accident on the British railway system that occurred on 11 June 1972 at approximately 21:35. Further Research He stated that he was thoroughly ashamed and that he had been celebrating a promotion to the position of Passed Fireman with his colleague who greatly assisted him. A public inquiry carried out into the cause of the accident was launched on 12 June 1972 by Colonel John R.H. Robertson that looked into the cause of the derailment. Initial reports suggest a person was hit by a motorbike. The second and third coach followed the first coach until relatively late into the derailment, with the coupling between the first and second failing around the end of the derailment. Wilsdon and Stokes were to sign on duty at Hither Green in person by 15:42 to catch a train as passengers to Ramsgate, transferring at Dartford. This procedure was considered practical and was allowed to remain in use, but it was agreed that the method Wilsdon used (where he casually booked on duty and for his own benefit of gaining two additional hours' pay by booking on at 15:22 instead of around 17:00 when he actually did leave home for work) was not appropriate and was to be stopped or prevented wherever possible. Owing to the large number of day-trippers booked for this customary annual works-outing, a pair of excursion trains were laid on to transport them to Margate and back. Stokes and Guard H. Atterbury. David Glasspool Collection, The main building on the "up" side was a carbon copy of the structure which still exists today at Bexleyheath. Well Hall station will be partially covered by the new Rochester Way relief road. The first coach followed the overturned locomotive but remained upright, the coupling failing quite late into the sequence. RSS Feeds By 1972 he was married with young children and living in Rainham, Kent - which meant he would usually have to make an almost two hour rail commute to his depot at Hither Green. An excursion train from Margate to Kentish Town derailed on a sharp curve at Eltham Well Hall station, Eltham, London. An excursion train from Margate to Kentish Town derailed on a sharp curve at Eltham Well Hall station, Eltham, London. Both men were subsequently suspended shortly afterwards, against which Wilsdon immediately appealed, claiming that the event was an isolated incident. As he did not need to be on duty until the afternoon, Wilsdon joined his two brothers for lunch at around 12:55, the three travelling to a local pub where they stayed until closing time just after 14:00. Links SYND 12-6-72 AFTERMATH OF ELTHAM TRAIN CRASH AP Archive 4.73M subscribers Subscribe 6 Share Save 2.5K views 7 years ago (11 Jun 1972) The aftermath scenes of a derailment of a excursion. Sometime between these two renaming occurrences, the goods yard acquired a five-ton crane. The secondman may not have been attentive because he had also been drinking, but he did not know the route and would not have realised that the driver was not braking for the curve when he should have been. The Eltham Well Hall rail crash was an accident on the British railway system that occurred on 11 June 1972 at approximately 21:35. The driver Robert Wilsdon and five passengers were killed, and 126 people were injured. When Stokes boarded the engine, he waited alone in the cab until around 18:25 when Wilsdon arrived and spoke about the preparations for the journey back to London. Despite his experience and long time working on the railways, Wilsdon had been reprimanded five times throughout his career. GitHub export from English Wikipedia. Royal Borough of Greenwich. +44 (0)20 7611 2222info@wellcomecollection.org, Except where otherwise noted, content on this site is licensed under a Creative Commons Attribution 4.0 International Licence, 1 photograph : photoprint ; sheet 15.3 x 20.2 cm, Injured in excursion disaster. The curve had a maximum permitted speed to be taken at 20 miles per hour (32 km/h) but the train was estimated to have been travelling at 65 . It also meant that his Supervisors at Hither Green would not see him in person. The driver Robert Wilsdon and five passengers were killed, and 126 people were injured. Most Wanted The next five coaches were derailed but the 10th, in which the guard was riding, was not. The rear end of the first coach came to rest up against the leading cab. United Kingdom. On Sunday 11 June 1972, a day-trip to Margate had been arranged for the employees (and their families) of British Rail's Midland Region based at the North London depot at Kentish Town. He immediately tried to signal to the driver to stop but was unable to gain Wilsdon's attention. The overgrown area behind the fence on the right was formerly the goods yard. As a result the heavy locomotive entered the curve at some 65 mph and, distorting the track and sharpening the curve immediately ahead of its wheels, overturned to the left and dragged the train after it into almost total derailment. It seems these splashes were too late and light to register in the cab. An excursion train from. The rear of the coach had been somewhat damaged by the fifth, sixth and seventh coaches passing by it, derailed but still on the track. The outbound journeys left Kentish Town around 0830, were completed uneventfully and the trains stabled at Ramsgate as planned. Of these penalties, three were fairly minor isolated offences (unauthorised absence in October 1960, persistent lateness in February 1961 and a "relatively minor driving offence" in February 1963) but two were serious offences, one of which resulted in a temporary suspension. The fourth coach had ended up roughly 90 degrees to the track, leaning over on its left side. Having been in operation for ninety years, today there is no trace of this station having ever existed, the site having fallen foul to a road widening scheme. The Eltham Well Hall rail crash was an accident on the British railway system that occurred on 11 June 1972 at approximately 21:35. This document is Crown Copyright, and is subject to the terms governing the reproduction of crown copyright material. British Rail staff who came in contact with Wilsdon on 11 June (his supervisor at Hither Green, depot staff at Ramsgate, Secondman Stokes, Railway Club staff at Ramsgate, Guard Atterbury, Stationmaster Arundell and his staff at Margate, Railman Fleming and Signalman Obee at Rainham) were all intensively questioned and gave evidence at the inquiry regarding the state of Wilsdon, to which all agreed that Wilsdon appeared perfectly fit and sober even as late as his unscheduled stop in Rainham, with the only person aware of Wilsdon already having drunk alcohol prior to reaching Ramsgate being Secondman Stokes, who considered him still fit and sober enough to drive the train.